Havengore has twin Gardner 8L3 engines.
During her re-fit in April 2006 it was found that the engines
needed significant work. The port engine required immediate
attention while the starboard engine was in better condition.
All of the work has been undertaken by Ray
and Michael Harrison of Gardner Marine Diesels. The work
undertaken by Gardner Marine Diesels is described below:
Port Engine:
The port engine was completely stripped down,
leaving only the top and bottom crankcase and crankshaft.
The dismantled parts were then removed from the engine room
via the small exit hatch using a chain lifting system. Main
components to be removed were:
- All 8 pistons
- All 8 conrods
- Fuel pump assembly
- 4 cylinder blocks (2 cylinders per block)
- 8 cylinder liners
- All 8 cylinder heads
The above items were transported back to our
workshop for cleaning and assessment. The following was
found:
- Large score marks were found on number
7 piston and liner and also smaller score marks were found
on numerous other piston/liner combinations. These score
marks denote a piston seizure, due to overheating of the
cylinders.
- Considerable sediment and cylinder block
erosion was found in the cylinder blocks. In this sediment,
a nut was found from the ram type water pump.
- On removal and dismantle of the water pump,
its internals were found to be in pieces, and as a result
it would not have been pumping any water around the engine.
- All wet liners were steam cleaned and
sandblasted, and were found to be worn.
- The cylinder heads were pressure tested
and the valves were tested. It was found that the valves
were not seating correctly and required attention.
- The bulkhead-mounted heat exchanger was
removed from Havengore and dismantled. A substantial amount
of sediment was found internally.
After the above assessment, the following
work was carried out:
- All 8 pistons were replaced. New L3 pistons
were not available at that time, so new later type L3B
pistons were used and machined to the tolerances required
by the L3. 8 new pistons ring sets were also used.
- Each cylinder block was thoroughly cleaned
and had 0.020” machined off each of its liner registers,
to remove any pitting.
- Copper shims of 0.020” thickness
were cut to replace the material machined off each cylinder
block.
- New L3 wet liners were sourced and purchased,
then honed. Each individual liner was lapped into the
top of each respective cylinder block to attain the correct
seating and therefore water tightness.
- The internals of the ram type water pump
that was found to be in pieces was sandblasted and re-assembled
using new valves.
- Each of the 8 cylinder heads were dismantled
and cleaned. The valves and valve seats were reground
and then lapped together again and again until an airtight
seal was formed. All inlet and exhaust valve guides were
found to be worn, so all were replaced. The heads were
tested again.
- The fuel pump damper was reconnected in
our workshop, and then realigned.
- All items were finally cleaned before
they were transported back on board Havengore.
Before the engine could be reassembled, the
top of the crankcase face had to be totally clean. The finding
of a thick gasket that had been placed between the crankcase
and cylinder blocks hampered this procedure. Due to this
surface being a face-to-face joint, the gasket had to be
scraped off and the face cleaned with cleaning solution.
The engine was then reassembled using the
new/cleaned parts. The piston to cylinder head clearance
was checked on all cylinders, and the engine reassembly
was completed.
Due to the poor state of repair that the original
Gilkes sea water pump was in, and the general bulky nature
of the cooling system, it was decided to install a new Bowman
heat exchanger/header tank unit, new Jabsco sea water pump
and replace the piping. This involved slightly altering
the water injection pipe into the exhaust.
Starboard Engine:
The starboard engine was found to be in better
condition than the port engine therefore little was done
to this engine but a major overhaul is planned for January
2007 during the next re-fit.
The cooling system was all replaced with the
new system as used on the port engine.
Both Engines:
- New custom built tachometers were fitted
in the wheelhouse for both engines, running off small
chain driven generators.
- Remote engine stops were installed
as per MCA requirements, as were injector pipe shields.
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